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authorAdam Ford <aford173@gmail.com>2018-01-25 14:10:37 -0600
committerTony Lindgren <tony@atomide.com>2018-02-14 08:35:51 -0800
commit74402055a2d3ec998a1ded599e86185a27d9bbf4 (patch)
tree32c183a3cb9eb8dab9ca581dca4fd3e05ab82053
parent64116257144bfbe744dd5b41bb0d160ccf65e339 (diff)
downloadlwn-74402055a2d3ec998a1ded599e86185a27d9bbf4.tar.gz
lwn-74402055a2d3ec998a1ded599e86185a27d9bbf4.zip
ARM: dts: LogicPD Torpedo: Fix I2C1 pinmux
The pinmuxing was missing for I2C1 which was causing intermittent issues with the PMIC which is connected to I2C1. The bootloader did not quite configure the I2C1 either, so when running at 2.6MHz, it was generating errors at time. This correctly sets the I2C1 pinmuxing so it can operate at 2.6MHz Fixes: 687c27676151 ("ARM: dts: Add minimal support for LogicPD Torpedo DM3730 devkit") Signed-off-by: Adam Ford <aford173@gmail.com> Signed-off-by: Tony Lindgren <tony@atomide.com>
-rw-r--r--arch/arm/boot/dts/logicpd-torpedo-som.dtsi8
1 files changed, 8 insertions, 0 deletions
diff --git a/arch/arm/boot/dts/logicpd-torpedo-som.dtsi b/arch/arm/boot/dts/logicpd-torpedo-som.dtsi
index b50b796e15c7..47915447a826 100644
--- a/arch/arm/boot/dts/logicpd-torpedo-som.dtsi
+++ b/arch/arm/boot/dts/logicpd-torpedo-som.dtsi
@@ -66,6 +66,8 @@
};
&i2c1 {
+ pinctrl-names = "default";
+ pinctrl-0 = <&i2c1_pins>;
clock-frequency = <2600000>;
twl: twl@48 {
@@ -136,6 +138,12 @@
OMAP3_CORE1_IOPAD(0x21b8, PIN_INPUT | MUX_MODE0) /* hsusb0_data7.hsusb0_data7 */
>;
};
+ i2c1_pins: pinmux_i2c1_pins {
+ pinctrl-single,pins = <
+ OMAP3_CORE1_IOPAD(0x21ba, PIN_INPUT | MUX_MODE0) /* i2c1_scl.i2c1_scl */
+ OMAP3_CORE1_IOPAD(0x21bc, PIN_INPUT | MUX_MODE0) /* i2c1_sda.i2c1_sda */
+ >;
+ };
};
&uart2 {